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After casting the grains I cast several strips of propellant for open air burn tests. After burning a couple of the strands, It seemed the propellant burned better than just plain KN/ER, but not much different from the last batch that used Fe2O3. Never the less, I was nervous about testing the propellant in a motor without doing any strand burn tests under pressure, so when I trimmed the grains to size, I reduced the total propellant weight.
When I went to assemble the motor, I was going to use a nozzle with a throat diameter of .32", then I chickened out, and used a nozzle with a throat diameter of .42".
Propellant Weight: .9226 pounds, 418.5 grams
Number of Grains: 4
Propellant Length: 9.875" (2.46875" each)
Diameter: 1.51"
Core Diameter: .63"
Kn:226, 248, 227
Nozzle Throat Diameter: .42"

Total Impulse: 47.18 pound seconds
Isp: 51.14
Burn Time: 2.753 seconds of recorded thrust
Peak Thrust: 31.14 pounds
Peak Chamber Pressure: ~200 psi
From looking at the thrust curve, it would appear the motor came to pressure quickly, it didn't. After pressing the ignition button down for some five seconds, I assumed the igniter had failed to light the motor, as I could see no smoke coming from the motor. I checked the power led on the launch controller, it was lit. I watched the motor for another 4 or 5 seconds, then finally a small stream of smoke appeared. Ever so slowly the stream of smoke increased, until after smoking some 20 seconds, the motor came to pressure and I could see thrust from my data acquisition screen on my PC. Once the motor came to pressure it seemed like a nice stable burn. After the thrust ceased, the motor continued to smoke for another 12 seconds or so. So I should have stayed with the .32" diameter nozzle, the Kn was way too low for this propellant.
I guess better safe than sorry, but this really was a waste of propellant. The only thing I really learned is that the sulfur didn't increase the burn rate dramatically. I'll have to repeat the test again using a smaller nozzle to increase the Kn.